Hi...
OK I'm using an 18M picaxe with a L293D motor controller. as far as I'm concerned I have set it all up correctly. When I test the L293D by applying a current to the inputs it acts like it should (bi-directional etc).
To test it I just did a VERY SIMPLE programme:
Running this an LED on output 3 it works fine... but as soon as I hook up the L293D to output 3 things start to go wrong...
It runs through the programme fine, but the second time it runs the programme, it seems to hang on the first HIGH. So the motor just keeps spinning?
I have grounded all extra input and outputs on th L293D, and am using 5V to run it all.
any ideas?
thanks in advance!
- Nick
OK I'm using an 18M picaxe with a L293D motor controller. as far as I'm concerned I have set it all up correctly. When I test the L293D by applying a current to the inputs it acts like it should (bi-directional etc).
To test it I just did a VERY SIMPLE programme:
Code:
main: high 3
pause 2000
low 3
pause 2000
goto main
It runs through the programme fine, but the second time it runs the programme, it seems to hang on the first HIGH. So the motor just keeps spinning?
I have grounded all extra input and outputs on th L293D, and am using 5V to run it all.
any ideas?
thanks in advance!
- Nick